Hi Rocketeer2001!
I joined this forum to ask you a question.
I just happened to be working on the same D9200 monitor. I fully recapped it, reflowed all the boards and it worked great, but it would start making a arc noise every so often; after heating up, it increased. I found if you take the factory sealed VR901 and turn it counter clockwise (raising the resistance) the arcing stops (this also scales the picture larger...
- note: I wrote down the original value before tweaking the pot). This is also demonstrated in one of the YouTube videos you linked.
Reason why I said "it worked great" was because I decided to do some poking around the board. My monitor is outside of a cabinet, and using a temperature gun I clocked the 2SC5144 getting close to 140f (60c). around this temperature I started getting wacky horizontal happenings (4 hours outside of the cabinet in an 85f (29.4c) ambient temperature room).
I decided it needed new thermal paste. So I took some MX-4 I had sitting around, took out the screw... that's when I noticed the screw for my 2SC5144 (Q418) wasn't tight at all. Without desoldering it, I bent the chip out of the way, used an alcohol wipe to remove the old white silicon, which was totally dry and cracking off both sides of the gray silicone pad, caked on some MX-4 on both sides and replaced it, this time cranking down the screw.
I restored power, and I got a squealing sound now from the monitor that was originally dead silent. Hmmm, was there a reason it was on there loose?
I loosened the screw... still squealing, and a burning smell (still in contact with heatsink); I then powered it up with the chip bent away from the heatsink (cleaning position) and the squealing stopped, it was back to normal. Was this a cracked solder joint? (nope).
I tried to put the screw in loose again, the squealing returned (each of these time, the monitor was only powered for a short period before disconnecting). Lastly, I pulled it away from the heatsink again, and when I powered it up, a FLAME shot from the screw hole! (anyone reading this, yes that whole thing was irresponsible, but it could survive momentarily without a heatsink, a flame shouldn't had shot from it... as far as I know).
I thought to myself, maybe I damaged the casing, cranking it down. The heatsink is just a plate, maybe a burr dug through the silicone pad?
After cleaning the chip, I found where the flame shot out. I felt the heatsink hole and there is a burr around the hole. I wonder if this had anything to do with it getting damaged? I wouldn't think bending the leads would had done it.
Question: Every time you replaced the 2SC5144, did you more than "snug" the screw for Q418 also?I think I read in a post that you were getting B+ (170v measured from either side R854) and the majority of your components were fine before the catastrophic failure.
Even though this 2SC5144 had a flame shoot from it, it still tests PERFECTLY! Both in a device like the one you shared, and the way Princess Prin Prin demonstrated.
I ordered a new 2SC5144 and will install it later this week. I plan on deburring the hole and just snugging the screw this time. I feel mine was already on its way out, but my mishandling helped it a bit.
Testing the surrounding circuit. Everything is fine. I cut power every time there was an oddity, and only left the screeching going until I could identify the noisy component.
I think, I'm only the 2nd person to work on this chasis. I'm sure I was the first to touch the 2SC5144 since factory.